Me being a severe hazard to anything electrical meant Dave being blackmailed into coming round and using his electrical wizardry! The first place of investigation was the actual switch itself and I persuaded Dave to take up the position that I was in the week before when I got the bolt from the offending electrics. i.e. one hand on the metal door handle and the other hand on gear lever, while he flicked the overdrive switch in with his thumb. He did say to me 'I wont get a shock from this will I?' to which I replied 'no of course not Dave'! Obviously, after jumping several feet in the air and all of the hairs in his nostrils smouldering, he realised I was lying! (What a fool, he should know me by now! :-) )
After various investigation and tracing of wiring to decipher what was working and what wasn't we then got the unique situation of losing all electrical power completely! No ignition, no interior lights, no clocks, no nothing! By now it was 6pm and Dave had the grumps anyway because he had a migraine, plus his other half had already sent him a 'Your dinners in the dog' type text. (Better than some of the lunatics I've been out with! I'd have more likely got a text saying 'your Dog's in your dinner!)
In fact, I knew he had the hump earlier when he was trying to explain some electrical workings to me that I just couldn't get, and he gave up and he told me 'F*ck off indoors and go and make the tea!'
Anyway, Sunday morning at 8am, I went back into the garage and after half hour of searching I found that a main wire in the loom had been cut into and rejoined with a scotch lock wire connector, but had come out. The offending wire was rejoined properly and all power was restored. Happy!
I then had a couple of hours off to go to the Battlesbridge Classic car show, but was back home again by 3pm to resume work on the car. Further delving underneath revealed that the inhibitor switch bracket (See pic below) had lost a bolt and was hanging down from the back of the gear selector. Therefore, the rod that is supposed to make contact with the switch when the car is in 3rd and 4th gear, wasn't touching it, so it then couldn't transmit any power down to the solenoid that operates the overdrive unit.
With this fitted back in it's rightful place, all appeared to be working well. I was still waiting for new gearbox cross member bolts to arrive, so I couldn't take the car for a test drive to see if it was working properly.
The bolts arrived on Wednesday and were fitted and Dave came round to join me for a test drive. The overdrive worked! Yay! for all of two seconds! Boo! A return to the garage revealed a faulty switch in the gear lever, so a new one from my spares tray was fitted.
The second test drive failed too. It was trying to come in but couldn't go in properly. The overdrive now appears to work electrically, but not mechanically. I haven't checked the gearbox oil levels in this car yet, so that will be this weekends task. I'm hoping that's all it is. (Common fault)
I really don't want to be pulling the gearbox out-They are too bloody heavy!
This is Dave about to perform a thorough examination, but I told him to leave next doors cat alone! Please note my immaculate and well organised work bench. Health and safety would be proud of this! :-)
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