Tuesday, 10 June 2025

Sunday 8th June. - Test drive and washy time!

 I had to get the cars out of the driveway this morning as I had finally sold my 2.6 Triumph engine on facebook market place and needed to bring out of the garage and up the driveway ready to load. I was quite glad it was going as I was getting tired of some of the dumb questions I had been asked. I.e. 'Is this a genuine Triumph engine, or did you make it yourself?'. I can do a lot of things in my garage, but casting brand new engine blocks isn't one of them! 😕

Anyway, the buyer arrived around 10.30 and I lifted the engine into the back of his Volkswagen Polo with my engine crane. (Which I had only folded down and put away in the shed the week before-Typical!) He was a nice guy and wanted the engine for his Triumph GT6. I gave him a few other Triumph bits that I had laying around and other than the Triumph Mk1 saloon I have in storage (which will be going up for sale very soon) I am more or less Triumph free now. 

Once he had gone, I fired up the Green Cortina and took it for a test drive. I only went local as its just had an engine rebuild and I didn't want to be too far away if anything went wrong. Luckily , nothing did go wrong and I had no nasty oil leaks either, so it looks like the recent work was worth the effort. 

Once back home I got the bucket and sponge out and gave it a good wash. It had got quite dusty and dirty from all that time sitting in the garage, so it was good to see it looking nice and clean again. Roll on Battlesbridge on Sunday! 😊




Sunday, 8 June 2025

Wednesday 4th June -Green Cortina Tuning!

 My friend Andy was coming round after work today for a long overdue beer and curry. I had some time to kill before he arrived, so I fitted a new set of spark plugs and altered the timing and set the firing order again on the Green Cortina. 

I also wanted to set the ignition timing with a strobe light, but I can't hold the strobe light and turn the distributor at the same time, so luckily, once Andy had arrived we were able to get that done. With the engine running smoothly we cleared everything up and quickly put the tools away as it had now started raining and the car was outside the garage. 

I was pleased how things had gone, but ideally I need to get the car out for a test drive. Hopefully, I'll have time on Sunday. With our work complete, Andy and I went for our much deserved beer and curry. And very nice it was too. 😊

Wednesday, 4 June 2025

Sunday 1st June - Little Easton Manor.

 The weather was predicted as being very hot and very sunny today which was just as well as Gavin, Andy & Sharon, and I had booked up to visit the breakfast meet at Little Easton Manor near Great Dunmow. 

I met Gavin at our usual spot and we had a slow drive over there. It was very slow actually due to getting stuck behind an artic, who then got stuck behind some cyclists for ages! Eventually we got to the show and were parked on the lake area. 

We then headed for breakfast in the form of a coffee and a sausage bap and started looking at the other cars. Good friends Andy and Sharon then arrived with another addition to their dog family and we found a table and had a good old catch up. It was a beautiful day and it was really nice to sit in the sun and just chill out and not be working on cars for a change. I should do this more often!


It was a nice atmosphere and everyone seemed to be enjoying themselves, but come 1pm I had to make a move. I had taken the Zetec Cortina, but it still has the problem of leaking oil from the diff. (Only slightly though)

I had spoken to the man who built it on Friday and he told me to disconnect the propshaft at the diff end and see if the flange nut is wet. If it is it means the flange seal has failed, but if it's leaking from inside the casing, then the casing seal has failed. 
So, once home I jacked the car up at the rear and disconnected the propshaft as instructed. I found that the flange nut was completely dry and all the leakage was from around the casing. After talking to my differential man he's told me that it can be done in the car so I don't have to remove the diff again, but he will need the car for about 4 to 5 days. So somehow I've got to find a way of taking it over to Baldock in Hertforshire, leaving it there and getting home again. What a pita! (Pain in the arse!)

This was the first time that I had taken the Zetec on a Motorway run (ok, fast A road) since having the differential ratio changed to 3:31. I have to say what an amazing difference! At 70 mph the revs per minute (RPM) is only 3,200 rather than the previous 4000. The car no longer seems like it's revving its nuts off and cruises quite nicely. I now no longer feel the need to fit a 5 speed gearbox in this car, which would have been a major job. So once the diff is sorted, I've got to be where I want to be with this car, so it should be relatively low maintenance. 



Tuesday, 3 June 2025

Saturday 31st May - Green car running and a new toy to play with.

 During the week, a new toy had arrived for me to play with. It was at a good price and I thought it might be a good bit of fun. It's a 1964 2 door Mk1 Cortina, but with a Nissan CA18DET engine. Which is a 1.8 litre, twin cam, 16 Valve, Turbo engine. Allegedly pushing 250bhp, but that's yet to be verified. It's also in Alan Mann racing colours which I've always liked.

I'd been to look at it the previous Saturday and when out on a test drive, it was the first time in a long, long time that I've sat in a car while the driver has put his foot down and I've thought to myself 'Holy Shit!' 

It has a digital speedo and when the seller put his foot down the numbers couldn't keep up with the speed. The scenery from my view in the passenger seat came towards me with an alarming acceleration that I'd not witnessed before. I thought my Zetec Cortina was quick, but this is something else. So, a deal was done and collection and delivery arranged. 
It's not completely to my liking, so for now it will go into the garage until it is. 

Anyway, back to the Green Cortina. I wanted to get this running today as I needed to get the new Cortina into the garage. So, I started on it as soon as I got home from shopping which was around 8am. Gavin arrived to help around 9am by which time I'd fitted the starter motor, connected the clutch cable and fitted the dust shield between the back of the engine and the bellhousing. 
We were soon ready to start the engine, but for some reason we couldn't get fuel through the electric fuel pump. Filling the fuel pump up manually seemed to bleed it and get it operating, but I then noticed that my throttle pedal was rock solid. Investigation of this revealed that the excess of the cable had found its way under the rocker box cover when I had tightened it down and was stopping it from moving! So with this corrected, we tried again. 
After various attempts, we had to alter the timing and swap some plug leads around. I'd said to the engine builder 'If you remove the distributor, can you mark it so it goes back in exactly the same place please, because it's spot on'. But he didn't. 

Eventually, we got it running good enough to drive, but it's still not 100%. By now I was running out of time as I had somewhere to be by lunch time, so we moved the cars around and called it a day. At least it's running though and more importantly, its not pissing oil out anywhere. it was good to see it out on the road as well as it's been in the garage far too long. I'm looking forward to taking it on a run with its newly rebuilt engine.



Monday, 26 May 2025

Monday 26th May. - A short drive out.

 It was supposed to rain today, but I woke up this morning to glorious sunshine. As a result, I put some of my outstanding work to one side and decided to go for a drive in my Zetec Cortina instead. 

Since changing the diff ratio to 3:31, this car drives a lot better. However, I'd suspected for some time that the front seal in the diff is slightly leaking and after jacking up the car on my return, it turned out that this is indeed the case. So I shall be speaking to the man who built it for me and see what he's got to say. It does annoy me when you pay a lot of money for someone to do a job and it isn't up to standard. The trouble is, it seems to be happening more and more these days. 



Saturday 24th May - Billericay Breakfast meet.

 Good friend Dave Harvey was down this weekend and we made arrangements to meet our other friend, Gavin at the breakfast meet. Luckily the rain that had been coming down since 5am had stopped so the meet was dry. I still think that put a lot of people off though as there wasn't many people there. 

One car that did catch my eye was a nice 2 door Ford Corsair GT. These are a very rare car now and I can't remember the last time I saw one. 


Dave and I left after a couple of hours as we had a prior arrangement on the Isle of Sheppey. (Well, I was going to look at another car!) The traffic on the Dartford Bridge was awful and it took far longer to get there than it should have. We spent an hour or so looking over the car and then went for a bag of chips on the seafront while we let the traffic die down a bit. 
Luckily, the drive home was traffic free and we made good time. Time for a nice cup of tea, then a visit to the pub! 


Friday, 23 May 2025

Tuesday 20th May - The engine's in!

 I finished work on time again today, so it was time to get a few more garage hours in, especially as I'm busy for the rest of the week and this would be the only chance this week.

I had to finish off fitting the steering column shroud and parcel shelf that had been extracted when I removed the steering box, but once this was done I turned my attention to the engine. I fitted the engine mounts as they had been removed by the engine builder and also re-fitted the clutch, making sure the bolts were tightened to the correct torque setting. 

The engine didn't want to go back in first of all, but with a bit of jiggery pokery it was soon in place. However, while the bell housing bolts lined up fine, the engine mounts didn't want to line up with the crossmember. After a bit of head scratching and thwarted efforts, I decided to remove the engine mounts from the block and swap them over. I mean, they looked exactly the same shape, so I didn't think they were handed, but I reckon they must be as things then became a lot easier and I was able to get the securing bolts in. 

As it was now 7.15pm, I called halt and went indoors for some dinner. I'm not sure when I will get a chance to get this finished off now as the rest of my week and the coming bank holiday weekend is looking quite busy, but any progress is still progress, so I was pleased with what I'd got done. To be continued! 😊